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NTSB says bolts on Boeing jetliner were missing before a panel blew out in midflight last month

Bolts that helped secure a panel to the frame of a Boeing 737 Max 9 were missing before the panel blew off the Alaska Airlines plane last month, according to accident investigators.
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FILE - This photo released by the National Transportation Safety Board shows the door plug from Alaska Airlines Flight 1282 on Jan. 8, 2024, in Portland, Ore. Investigators say bolts that helped secure the panel on the Boeing jetliner were missing before the panel blew off the plane in midflight last month. The National Transportation Safety Board issued a preliminary report Tuesday, Feb. 6 into the Jan. 5 accident. The loss of the panel forced pilots of the Alaska Airlines Boeing 737 Max 9 jet to make a harrowing emergency landing. (National Transportation Safety Board via AP, file)

Bolts that helped secure a panel to the frame of a Boeing 737 Max 9 were missing before the the Alaska Airlines plane last month, according to accident investigators.

The National Transportation Safety Board said Tuesday a preliminary report on the Jan. 5 incident that the lack of certain damage on the plane indicates that all four bolts were missing before the plane took off from Portland, Oregon.

Without the bolts, nothing prevented the panel from sliding upward and detaching from 鈥渟top pads鈥 that secured it to the airframe.

The Alaska Airlines pilots were forced to make a harrowing emergency landing with a hole in the side of the plane, but no serious injuries were reported.

The NTSB report included a photo from Boeing, which worked on the panel called a door plug, that showed that three of the four bolts that prevent the panel from moving upward are missing. The location of a fourth bolt is obscured by insulation.

The preliminary report said the plane arrived at Boeing鈥檚 factory near Seattle with five damaged rivets near the door plug, which had been installed by supplier Spirit AeroSystems. A Spirit crew replaced the rivets, which required removing the four bolts and opening the plug.

The report did not say who removed the bolts. It said that a text message between Boeing employees who finished working on the plane after the rivet job included the photo showing the plug with missing bolts.

Sen. Tammy Duckworth, D-Ill., was upset at Boeing's lack of documentation about who did what and when the bolts went missing.

鈥淭hey didn't write any of this down,鈥 she said in an interview. 鈥淚t is very much Boeing's responsibility, absolutely, but I'm concerned that we may have multiple points of failure here.鈥

The NTSB did not declare a probable cause for the accident 鈥 that will come at the end of an investigation that could last a year or longer.

鈥淲hatever final conclusions are reached, Boeing is accountable for what happened,鈥 CEO David Calhoun said in a statement. 鈥淎n event like this must not happen on an airplane that leaves our factory. We simply must do better for our customers and their passengers.鈥

Investigators said they were still trying to determine who authorized the Boeing crew to open and reinstall the door plug.

Safety experts have said the accident could have been catastrophic if the Alaska jet had reached cruising altitude. The decompression in the cabin after the blowout would have been far stronger, and passengers and flight attendants might have been walking around instead of being belted into their seats.

When Alaska and United Airlines began , they reported finding loose hardware including loose bolts in some of the door plugs. Boeing said none of the other Alaska and United Max 9s have been discovered to be missing the critical bolts.

The incident has added to questions about manufacturing quality at Boeing that started with the deadly crashes of two Max 8 jets in 2018 and 2019, killing 346 people. In 2021, Boeing with the Justice Department to avoid criminal prosecution on a charge of conspiring to defraud government regulators by failing to accurately describe a flight-control system that was implicated in the crashes.

The Federal Aviation Administration is investigating whether Boeing and its suppliers followed proper safety procedures in manufacturing parts for the Max. The FAA has barred Boeing from until the agency is satisfied about quality issues.

FAA Administrator Michael Whitaker said Tuesday that his agency is about halfway through a six-week audit of manufacturing processes at Boeing and Spirit, its key supplier on the Max. He said the agency is confronted with two questions: What鈥檚 wrong with the Max 9? And, 鈥渨hat鈥檚 going on with the ?鈥

Spirit, which Boeing spun off as a separate company nearly 20 years ago, said in a statement that it is reviewing the NTSB preliminary report and is working with Boeing and regulators 鈥渙n continuous improvement in our processes and meeting the highest standards of safety, quality and reliability.鈥

The plug that broke off Alaska flight 1282 is used to seal holes left for extra emergency doors. Alaska and United don鈥檛 have enough seats on their Max 9s to trigger a requirement for the extra exits, so they tell Boeing to install plugs instead because they are lighter and cheaper than doors.

Alaska Airlines has estimated the grounding of its 65 Max 9s will , and it expects to be compensated by Boeing. United said the grounding would cause it to and plan for a future without new, larger Max jets that have not yet been approved by the FAA.

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This story has been corrected to note that a Spirit AeroSystems crew, not a Boeing crew, repaired the rivets.

David Koenig, The Associated Press